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Swissair Flight 306

Swissair Flight 306
SR Caravelle.jpg
Swissair's HB-ICX, sister aircraft to the aircraft HB-ICV lost in the accident.
Accident summary
Date September 4, 1963
Summary In-flight fire leading to hydraulic failure and loss of control
Site near Dürrenäsch, Switzerland
47°19′N 8°09′E / 47.317°N 8.150°E / 47.317; 8.150Coordinates: 47°19′N 8°09′E / 47.317°N 8.150°E / 47.317; 8.150
Passengers 74
Crew 6
Fatalities 80 (all)
Aircraft type Sud Aviation SE-210 Caravelle III
Aircraft name Schaffhausen
Operator Swissair
Registration HB-ICV
Flight origin Zurich Airport
Stopover Geneva International Airport
Destination Fiumicino Airport

Swissair Flight SR306, a Sud Aviation SE-210 Caravelle III, named Schaffhausen, was a scheduled international flight from Zürich to Rome, via Geneva. It crashed near Dürrenäsch, Aargau, on September 4, 1963, shortly after take-off, killing all 80 people on board.

Zurich Airport was in dense fog when the plane was due to take off at 06:00 UTC. At 06:04 the flight was allowed to taxi to runway 34 behind an escorting vehicle. At 06:05 the crew reported that they would taxi halfway down runway 34 to inspect the fog and then return to the take off point. This was done using high engine power in order to disperse the fog. Around 06:12 the aircraft returned to runway 34 and was allowed to take off, which it did 06:13, and started to climb to flight level 150, its cruising height.

Four minutes later people on the ground noticed a white trail of smoke coming from the left side of the aircraft. Shortly after, a long flame erupted from the left wing. Around 06:20 the aircraft reached a height of about 2700 m. It then began to descend, entering a gentle left turn before losing height more quickly. It then went into a final, steep dive.

At 06:21 a MAYDAY message was issued. At 06:22 the aircraft crashed into the ground on the outskirts of Dürrenäsch, approximately 35 km from Zürich Airport.

The aircraft's brakes overheated due to the application of full engine power during taxiing. This caused the magnesium wheels to burst, one of them on the runway prior to departure. Upon retraction of the landing gear, the hydraulic lines in the gear bay were damaged. This was caused either by the wheels that had exploded, or the bursting of the other wheel rims during the climb. Subsequently, spilled hydraulic fluid ignited when it came in contact with the overheated landing gear rims. The fire damaged the gear bay, followed by the wing. Finally losing its hydraulic pressure, the aircraft became impossible to control. The cabin and the cockpit were filled with smoke, adding to the predicament of the crew. Control of the aircraft was lost totally at around 06:18, and the ensuing final dive and impact destroyed the aircraft.


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