Launch of an Atlas-E missile
|
|
Function |
ICBM Expendable launch system |
---|---|
Manufacturer | Convair |
Country of origin | United States |
Launch history | |
Status | Retired |
Launch sites |
LC-11 & 13 CCAFS OSTF-1, LC-576 & SLC-3, VAFB |
Total launches | 48 |
Successes | 33 |
Failures | 15 |
First flight | 11 October 1960 |
Last flight | 24 March 1995 |
The SM-65E Atlas, or Atlas-E, was an operational variant of the Atlas missile. It first flew on 11 October 1960, and was deployed as an operational ICBM from September 1961 until April 1966. Following retirement as an ICBM, the Atlas-E, along with the Atlas-F, was refurbished for orbital launches as the Atlas E/F. The last Atlas E/F launch was conducted on 24 March 1995, using a rocket which had originally been built as an Atlas E.
As fully operational ICBMs, the Atlas E and F, which differed only in guidance systems, had upgraded engines and inertial control instead of the Atlas D's radio ground guidance. The ignition system was also different from the one used on the D-series, which used a "wet" start, meaning that the propellants were injected into the combustion chamber prior to ignition, and a hypergolic igniter on the fully developed version. The Atlas E/F for comparison used pyrotechnic cartridges and a dry start (ignition coming before propellant injection) for an extremely rapid ignition that required no hold-down time on the pad to prevent combustion instability. The booster engines had separate gas generators unlike the Atlas D which had one gas generator for both engines.
Atlas-E launches were conducted from Cape Canaveral Air Force Station, at Launch Complexes 11 and 13, and Vandenberg Air Force Base at OSTF-1, LC-576 and SLC-3.
The Atlas E testing program commenced on October 11, 1960 when Missile 3E was launched from Cape Canaveral's LC-13. At around 40 seconds into launch, the sustainer hydraulic system lost pressure. After booster jettison, the missile lost attitude control, tumbled, and broke up at T+154 seconds. On November 30, the second attempt, Missile 4E, repeated the same failure except that the missile remained structurally intact until impact in the ocean. Missile 8E on January 24, 1961 lost roll control due to aerodynamic heating shorting the vernier pitch control servo, a problem that had not occurred since the early Atlas A tests. Missile 9E on February 4 was successful. Missile 13E on March 14 experienced problems with the propellant utilization system and prematurely depleted its LOX supply. Missile 16E (March 25) experienced yet more valve problems, this time causing loss of pressure helium and making it impossible to jettison the booster section. The missile was dragged down by the weight of the spent booster engines and fell short of its intended range, also the propellant utilization system malfunctioned again and caused the engines to run fuel rich.