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GX (rocket)

Galaxy Express (GX)
GX rocket.jpg
GX (Shown with Atlas III first stage as in early development)
Function Medium expendable Launch vehicle
Manufacturer Galaxy Express (JAXA/ULA/IHI)
Country of origin Japan/United States
Size
Height 48m
Diameter 3.3m
Mass 190,500 kg
Stages 2
Capacity
Payload to LEO 3,600kg
Payload to
800km SSO
1,814kg
Launch history
Status Cancelled 2010
Launch sites Vandenberg SLC-3E
First stage - Atlas CCB
Engines 1 RD-180
Thrust 4,152 kN (933,406 lbf)
Specific impulse 311 sec
Burn time 253 seconds
Fuel RP-1/LOX
Second stage - GX
Engines 1 liquid
Thrust 118 kN
Specific impulse 323 sec
Burn time 480 seconds
Fuel LNG/LOX

GX was a design for an expendable launch system intended to compete in the commercial satellite launch sector. The system had developed by Galaxy Express Corporation, a joint venture between IHI Corporation (IHI), the Japan Aerospace Exploration Agency (JAXA), United Launch Alliance (ULA), Lockheed Martin Corporation (LM) and several other Japanese companies.

The GX design uses a two-stage rocket. The first stage would have been the Atlas Common Core Booster, currently used as the first stage of the Atlas V rocket, which would have been provided by United Launch Alliance. The second stage was to be a newly designed stage produced by IHI, using liquefied natural gas as fuel and liquid oxygen as an oxidizer. The GX would have been the only space vehicle to use that combination of fuel and oxidizer.

The Japanese government finally abandoned the GX program in December 2009. Galaxy Express disbanded around March 2010.

The GX program began as an effort to upgrade Japan's J-I rocket, which launched only once. Thus, GX was originally known as J-II, albeit briefly. For a time, the program was termed J1-Upgrade, before finally settling on the current name in January 2003.

JAXA reported that a full-scale second-stage engine had been successfully test-fired in October 2007. JAXA was developing this engine, the responsibility for which was planned to eventually be turned over to the Galaxy Express venture.

In late December 2007, The Yomiuri Shimbun newspaper reported that the GX program was being subjected to a thorough review, mainly because of unexpectedly high additional costs. It also erroneously claimed that ULA partner Lockheed Martin had discontinued production of the first stage engine, thereby requiring a redesign, likely costly, to move to another engine. The paper said that the 15 billion yen that JAXA requested for the GX project was eventually slashed to 5.6 billion yen in the Fiscal 2008 budget.


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